Author Topic: New Problem, never seen it before. top colour cracking when pulling off platen  (Read 2700 times)

Offline Inkworks

  • !!!
  • Gonzo Member
  • ******
  • Posts: 1761
  • Pad&Screenprinter
Here is what I can tell you:

Base coat is a 156LX, we've tried two different whites and various states of flashed, no difference. We even thrie 2 coats of base white, no difference. one white was QCM fast flash, which is our normal cotton white, not a new bucket. the other was a sample of Triangle cotton white. no difference.

Top coat (maroon) is QCM W.O.W Bright Red with a bit of QCM W.O.W Black. 320 grams to 20 grams if that helps. neither are new buckets, both have had lots of use. it was printed through a 230, but then switched to a 156, both showed the same problem.

When pulling the Gildan 2000 Black shirt from the platen, the maroon fractures and ends up looking like a distressed print. flashing the maroon cures this problem.

we've tried all sorts of different squeegee pressures and angles too.

picture shows flashed and unflashed samples after pulling

wtf?

Wishin' I was Fishin'


Offline kingscreen

  • Gonzo Member
  • ******
  • Posts: 1161
In my experience, this is typically the result of too much tack along with over flashing.
Scott Garnett
King Screen

Offline tonypep

  • Ludicrous Speed Member
  • *******
  • Posts: 5683
I agree. This can also happen with a DC UB

Offline Homer

  • !!!
  • Gonzo Member
  • ******
  • Posts: 3205
In my experience, this is typically the result of too much tack along with over flashing.

agreed, over flashing on the base...
...keep doing what you're doing, you'll only get what you've got...

Offline Inkworks

  • !!!
  • Gonzo Member
  • ******
  • Posts: 1761
  • Pad&Screenprinter
Well we're at about 2 seconds flash, nothing different ink or flash-wise than we've done for the last 3 years, hundreds and hundreds of jobs.

It was a somewhat new bucket of QCM Fast Flash, but we have run several jobs with it without issue, but QCM quality has gone to complete poop after the Rutland buy-out.
Wishin' I was Fishin'

Offline Inkworks

  • !!!
  • Gonzo Member
  • ******
  • Posts: 1761
  • Pad&Screenprinter
I thought too much tack too for a while,because we had just run tech shirts, but now we've tried platens with almost no tack left on them.

I'm running atest with 1.2 seconds of flash (quartz flash on auto) if I can get it to cure, but like I said, these aren't seeing any more flash than normal, and less than many jobs.
Wishin' I was Fishin'

Offline Inkworks

  • !!!
  • Gonzo Member
  • ******
  • Posts: 1761
  • Pad&Screenprinter
Okay, actually turned the flash down to the point where it wasn't flashing fully and base white ink was transferred to the maroon screen and still seeing a bit of cracking.
Wishin' I was Fishin'

Offline DCSP John

  • Sr. Member
  • ****
  • Posts: 340
try running the shirts around again so the last color has been flashed as well
So, when pulling shirts all ink colors  have been gelled. Not what you want to hear on a big job,
but thats what we've done when this happened to us..

V/r - John

Offline jvanick

  • !!!
  • Gonzo Member
  • ******
  • Posts: 2477
or if you have an extra flash, flash at the unload station... probably be faster than running them around the press a 2nd time.

Offline Inkworks

  • !!!
  • Gonzo Member
  • ******
  • Posts: 1761
  • Pad&Screenprinter
yeah, it's not a huge job, but I don't even want to tear it down until I lick the problem. We'll try switching to a different top color before tear-down. This shouldn't be related to using 156LX as a base coat mesh right? We've run 230 T mesh base whites without this issue.
Wishin' I was Fishin'

Offline Screened Gear

  • Gonzo Member
  • ******
  • Posts: 2580
Your maroon is the problem. The orange is not fracturing. I don't remember what it was but I had this happen on a job also. I hate printing maroon on PFPF under base.  I don't remember what I did to fix it for sure. I didn't change my flash much so I don't think that was it. Try running the maroon with less pressure so you lay down more ink. That should fix it.

Offline Inkworks

  • !!!
  • Gonzo Member
  • ******
  • Posts: 1761
  • Pad&Screenprinter
We've done that, we actually went from a 230 maroon screen to a 156 for just that purpose.
Wishin' I was Fishin'

Offline Screened Gear

  • Gonzo Member
  • ******
  • Posts: 2580
We've done that, we actually went from a 230 maroon screen to a 156 for just that purpose.

Well then I have nothing. I do remember this happening, like yours only with the maroon. Are you PFPF the underbase for the maroon? That I think is the problem that started this for us. I only remember it happening for the first 20 or so. Then our changes on press fixed it. You know it may have not been the changes we made but the fact that our boards got hot. Where your boards hot when printing this job?

This can easily be fixed with adding a flash before the unload station like some have said. Like you I want to know why it happened not just make it go away.

Offline screenxpress

  • !!!
  • Gonzo Member
  • ******
  • Posts: 2434
Almost looks like the underbase is rejecting the top coat of maroon.  Did you get them to shake hands before starting?  j/k
Anything important is never left to the vote of the people. We only get to vote on some man; we never get to vote on what he is to do.  Will Rogers

Offline Inkworks

  • !!!
  • Gonzo Member
  • ******
  • Posts: 1761
  • Pad&Screenprinter
Well after a phone call to Sonny/Printficient (Thank-you!) we seem to have found the culprit!

Pallets were sporting a coat of Sprayway Fast Tack 384 Super flash mist from the previous run of tech shirts. not a ton, and not enough to cause a problem with pulling the shirts off, but basically may have been causing some sort of chemical/offgassing thing.   Fresh pallet tape and a change to Sprayway 83 Web adhesive cured the problem, even though overall tack wasn't reduced, in fact it was probably increased.

We ran the job (96pcs.) and flashed after the maroon, but after that I left it set up and started to eliminate potential causes as I sure didn't want to run into this under a tight deadline.
Wishin' I was Fishin'